COOLflow Case Study 115
The SS Universe Explorer Achieves a 6% Fuel Savings by Increasing Boiler Efficiency with COOLflow Technology
The Situation
The SS Universe Explorer is a 23,500-ton cruise ship that
serves more ports of call than any other cruise line plying
Alaskan waters. One of its other functions is to serve as a
floating campus for the "Semester at Sea" program offered by
the University of Pittsburgh. The cost of fuel is the single
largest expenditure for any seafaring vessel in a hyper-competitive
environment, impacting both cruise prices and
profit margins. To this end, any fuel savings realized by ships
like the Universe Explorer directly affect their bottom lines.
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| The SS Universe Explorer |
The shipping industry is not governed by emissions
regulations; however, ships are restricted in regards to
limiting visible emissions while in port and often times
within sight of land. Along with these restrictions, the fuel oil
burners on the ship must also meet several important
operational requirements, which include high burner
turndown and complete carbon burnout with low excess air
levels at all loads. The Universe Explorer needed to increase
its operating efficiency without increasing visible emissions or
compromising operational capability.
The Boilers
The Universe Explorer is operated by three main,
Foster Wheeler marine D-type boilers, two of which have
left-hand configurations and one that has a right-hand
configuration. Design operating conditions are 105,000 lbs/hr
of superheated steam at 600 psig and 855°F. Each boiler uses
four cast iron TODD® D-register burners that fire light oil in
a pattern of two over two.
The TODD Solution
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| Fig. 1: : |
COOLflow Physical Modeling |
Engineers from John Zink's TODD Combustion Group
visited the Universe Explorer at its Vancouver, B.C., port to
gather information and assess the conditions of the units to
develop a solution that addressed the ship's efficiencies and
emissions. In order to design low-cost retrofits for the boilers,
the burner engineers recommended a COOLflow physical
modeling study on the combustion air supply systems of the
boilers. The engineers then gathered additional information to
construct a scaled physical model, (Fig. 1) which was used to
determine existing airflow patterns and design the solution.
The solution took the form of baffles and turning vanes to
improve airflow distribution within the windbox and to the
burners.
During their visit to the Universe Explorer, the engineers
observed that the existing "air casing", or windbox, was not
deep enough to contain the new required baffles. To remedy
this, an 8'x8' "window" was designed to make the burner area
accessible. The "window" provided an additional benefit by
enhancing combustion air residence time through the
windbox.
The Universe Explorer follows typical routes from year
to year during its "Semester at Sea" voyages, so fuel usage data
can be easily compared between voyages using fuel bunkering
reports. To verify that the airflow modifications were
successful, baseline data was gathered from the previous cruise
fuel reports and compared to post-retrofit fuel usage data.
The TODD Result
After the model was completed, the solution was
implemented along with the installation of new TODD D-register
burners of the same design, which were required due
to the windowing of the windbox. Since two boilers had
identical configurations and the third was a mirror image, the
modelers simply provided a mirror copy of the baffle
arrangement for the third unit. Much of the old fuel burning
equipment was modified and reused.
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| Fig. 2 |
Before correction, the mass flow was 45% deficient for
one of the bottom burners. Large areas in the bottom burners
had no air (-100% airflow). In fact, the modeling indicated
reverse flow through areas of the bottom, right-hand corner
burner (Burner No. 1) as seen in Fig. 2. This coincided with
the burner that previously experienced inexplicable
premature diffuser failure. The baffle solution designed
ensured that each burner was provided with adequate
airflow. As Fig. 3 indicates, the mass flow of air to each
burner was brought to within +/-1% of average from an
uncorrected condition of +/- 55%. Figure 4 indicates the
peripheral distribution was brought to within +/-9.6% for all
of the burners from an uncorrected condition of +/-112%.
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Fig. 3
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| Fig. 4 |
Improvements in airflow distribution within the
windboxes enabled the boilers to operate at reduced excess air
rates, which provided a gain in boiler efficiency and resulted in
reduced fuel consumption. Following the retrofit, the ship's
chief engineer helming a "Semester at Sea" reported fuel
savings of between 6% to 7% when compared to historical fuel
usage data for the identical route. The firesides of the boiler
also remained cleaner than on previous voyages, indicating an
improvement in carbon burnout.
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